Fusion file (with most recent tool paths): https://a360.co/2Ul2tu2
After that, I ran into Ryan and he realized that the cross
shape probably wouldn’t add any sort of value to the setup, to which I realized,
he was totally right. So now, I had a big piece of material that would not have
a parameter cut done to it…so it’s just taking up space now. I continued
forward with the dowel holes. I first made the holes into the material, and
then touched off the z-axis on the spoil board to get the same exact holes, in
the same exact place as cut into the pink foam. The picture below shows the hole drilling.
Something strange happened during the hole cut though. I had
initially programmed the holes to be a quarter inch in diameter, but they came
out to be less. So I went into the program, made them bigger (about 0.30 inches)
and ran the hole cutting program on the material and the spoil board again. Of course
I re-ran the program prior to making the spoil board holes since I couldn’t move
the pink foam or else everything would be screwed up. The holes looked more appropriately
sized, and then I saw that the dowels were actually around 0.33 inches in
diameter, so they wouldn’t fit…so I ran the program once more. Something even
weirder happened during this run, the program didn’t put the holes in the same
spot even though I didn’t change anything! Everything was kept the same but
yet, the holes were misaligned. I never figured out why that happened, but it
never happened again (so yay?).
After all that nonsense, I finally flipped my foam over and
plopped the dowels in to retain the correct origin. Once I started the top cut,
I saw that it wasn’t exactly in the middle like the bottom cut (look at the
picture to the left). I was too deep so I wanted to see what would
happen. Well, after the top cut finished, I saw exactly was happened. The
figure below to the right is the final cut of round one… it was a nice and easy
failure. So I went back to the program to see what was going on, and I saw that
my stocks within the different setups were not equal. That probably wasn’t the
main culprit but it certainly didn’t help. Then I realized that the origins
within the different setups were not along the same edge…that was no good.
So I went ahead and fixed all of that and made the stock and
origins consistent. I also made the material much smaller and the dowel holes
toward the corners so it would be easier to locate. Upon these fixes, I ran it
again! The picture below shows the bottom/hole/top cuts made. The
dowels served their purpose, everything was aligned, and all was right in the
universe. The last picture shows the final pink foam product, pretty cool. I
sanded down the edges to make it look more slick.
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